
2012 Calendar
of Events
A journey to world class
The Samlesbury brewery, now owned by Interbrew, has used its Asset Care programme as
a key tool for pursuing cost reduction through more intensive use of plant
Samlesbury is one of the largest
breweries in Britain, and has
the capacity in its fermentation
and maturation vessels to
supply a pint of beer to every UK
resident. As a 30 year old site in an
increasingly competitive industry, cost
reduction through improved asset
utilisation was seen as a major issue for
the future, and the vehicle for driving
this was employee involvement
through application of total productive
maintenance (TPM) principles.
However, Samlesbury had previously
tried TPM and failed.One anecdote
told of an autonomous maintenance
exercise which had resulted in a major
item of equipment being covered with
tags which were later just painted over.
This time, the company would take a
more pragmatic approach, aimed mainly
at involving shift teams in improvements
in hygiene and workplace organisation,
tapping into the workforce’s unused
expertise. Benchmarking visits to look
at employee involvement confirmed
that 5S principles were a very powerful
way to involve people, but management
were concerned not to brand the
initiative, but to develop their own
approach.
A process improvement manager,
Mark Holmes,was appointed to initiate
and run the programme,which became
known as simply Asset Care (a banner
that could include almost any activity).
As a pilot, the company chose the older
bottling line 4 rather than the new
high-profile line 3.The advantage of
this was that line 4’s equipment had
deteriorated significantly, but also that
the line was not on any high-profile
walkways – it was somewhere the
company could safely experiment.
![]() The Keg Racking area. |
External trainers from Productivity
Europe,whom general manager
Richard Jenner had also used while
working at Unilever,were used to
deliver the initial training,which
comprised a ‘down day’when two shifts
were brought in together, given an
overview of the approach and then
audited their assigned area and
developed an improvement plan.The
approach was based on 5S principles,
but using 5S for improvement, not just
housekeeping.
This meant that the teams, as well as
conducting 5S audits, produced a 30-
problem list of issues which were then
prioritised and categorised as ‘do’s’
(improvements the teams could make
immediately),‘fixes’ (those that required
some small resource or time slot
planning) or ‘redesigns’ (those that
required longer term project work).
Teams were encouraged to look for
low-cost, low-tech, people-friendly
improvements that resulted in a very
large proportion of do’s and fixes rather
than redesign projects.At the end of the
implementation day the teams presented
their findings and plans to management
with their prototype activity board.
The major learning from the pilot
was that although a classical seven-step
autonomous maintenance programme
had initially been considered, it was
more effective in this environment to
start with 5S in the area and then apply
5S to equipment using the 30-problem
list and action planning system they had
developed.Other TPM techniques, such
as measuring OEE (overall equipment
effectiveness) and developing operator
maintenance standards were simply
brought in as part of the Asset Care
process. Bill Thomas and Steve White
were appointed as internal Asset Care
coordinators; they still use the 5S image
of the shed and the supermarket – are
we working in a dirty, disorganised shed
or a clean, visually managed
supermarket?
Communication across shifts
remained a difficulty – each shift was
responsible for setting the standard and
making improvements for a specific
area, but all shifts then needed to work
to the standard.This necessitated a lot of
work on visual management and
control. In order to generate ownership,
activity boards were not totally
standardised but were created by each
team,within Asset Care guidelines and
principles. Each team nominated an
Asset Care facilitator,who took
responsibility for managing the 5S
activities alongside the team leader.
Supernumerary operators were also
provided on day shift to free people up for improvement work.
The line 4 pilot was launched in
September 2000. By January 2001 the
company had enough confidence in the
process to launch in other areas. In 2001
line 4 rose to within one per cent of
the efficiency of the much newer line 3,
a notable achievement,which has
secured investment in new secondary
packaging equipment this year.
Two roll-out areas with significant
achievements are Keg Racking and
Beer Recovery, both unglamorous areas
of operation.Racking basically cleans
and fills kegs, and Beer Recovery
processes and recovers yeast.
Asset Care has transformed Racking
into a shining example of employee
involvement.Using 5S principles the
area has improved its housekeeping
audit scores from the 20s to the 70s and
has increased efficiency from 57 to 62
per cent.The plant has hit 70 per cent
on some shifts, a level which racking
manager Paul Brow believes is
sustainable; only an inability to get
enough kegs loaded to the line stops it
being achieved regularly.The teams have
a focused improvement war room to
look at particular issues, such as raising
the efficiency of the ‘core’ plant.
This progression from 5S to focused
improvement is a deliberate strategy, and
Mark Holmes believes the sequence is
important. 5S is aimed at increasing
involvement and allowing teams to do
away with their ‘gripes’,many of which
do affect performance. Focused
improvement then looks at specific
issues using traditional problem-solving
tools such as cause and effect diagrams.
Beer Recovery is a good example of
this.An initial 5S audit of the Beer
Recovery area recorded a score of 7
and generated 40 do’s, 5 fixes and 3
redesigns. Four weeks later the audit
score was 21, and improvements were
well under way.Management responded
to this by authorising a focused
improvement project on the alcohol
recovery plant,which had been
identified as a constraint on the brewing
process, in parallel with the 5S work.
Using a cause and effect diagram, the
teams identified three areas of focus –
methods (understanding of the process),
the process itself, and plant reliability.To
tackle the methods issue, new written
standards were developed by the teams
and everyone trained in the correct
operating procedure. In terms of the
process itself, it was again traced to a
lack of standardisation of yeast dilution
and so standards for the operation were
developed by the team to counter this.
Plant reliability was then tackled
through the Asset Care process, raising
22 improvements on the alcohol
recovery plant alone.
Over the four-month project, the
workplace audit score was raised to 55
per cent and 86 improvements were
implemented.The focused improvement
project itself resulted in a cost saving of
nearly £90,000.
Mark Holmes believes they are 30
per cent of the way to being world
class,with the process consolidated in
some areas.The challenge now is to
ensure that all areas are developed to the
same standard and the site focus is on
the issues that improve performance.
Two points Mark makes are that teams
will always want to move faster than
your ability to support them, so
managing expectations is important; and
that the best ideas are low cost – the
company has spent money on asset care
improvements, but that money has gone
a long way.■
Process equipment, following 5S implementation and clearning (inset) |




